The new Rolling Stock shed is complete at Lakers
Siding and this now will provide the railway with
the facility of keeping its carriage stock and other
equipment out of the sea air. The next stage
is to lay the track into the shed and this is
now under way.
Another notable mile stone is the fabrication and erection of a
new smoke box tube plate for the boiler of T251. Once the
tube plate was fabricated it was riveted to the
boiler shell. Initially, the plate was bolted to the shell and
the rivets were placed in a circular manner replacing
every second bolt to ensure that the
plate was distortion free.
The new platform at Swan Bay had great use when it
was used as a park and ride facility for the
Seafood Feast held on the Queenscliff foreshore. Over 200
return journeys were made. The platform is some 2 km
from the town and both rail motors were
used in multiple unit.
This was possible with the return to service
of DP28 after a long refurbishment. Multiple uniting with
DP29 provides the railway with 100 seats for such
shuttles. The railway has received the frame of
South Australian Dolly Varden guards van 7550 which it had
previously owned. The van was purchased in 1982 in
unusable condition and then went to Puffing Billy who
found that they could not use it either.
The body was scrapped and the frame made available to
the Bellarine railway who hope to rebuild a new van on the
frame in the future.
Carriage DB46 has been dual braked to operate on
both air and vacuum braking. Carriage ABL14 has been
restored and is now complete. Locomotive T251 has
been placed in the workshop siding to allow its
restoration to proceed .
The railway had as its guest the Hon Justin Madden,
Minister for Planning in his capacity as Heritage
Minister. He was visiting to view the work of the
Heritage Care volunteers and to inspect the
progress on the restoration of 53RM. The Minister's
attention was drawn to the need to provide
covered accommodation for the railway's rolling stock to guard
against the weather and to deter vandals.
A major effort on the track in Daylesford resulted in the
replacement of 78 point timbers, the re-seating of 3 point
levers, the foot crossing re-laid and a bent point blade
straightened.
A new male toilet and lamp room are being built at a
cost of $102,000 with a grant of $68,000 from the State
Government with the balance of funding from the Shire Council,
the DSCR together with work in kind by the
railway. The present toilets will become the female
toilet on completion of the male toilet.
The railway suffered with a spate of
broken windows and a large amount of time has been
spent in repairing the damage. Rail Motor 91RM has
commenced the long awaited roof repairs. The motor
has been in service on the railway for 18 years and
has travelled over 50,000 km on the CHTR.
32RM: Work is continuing and the newly fitted ceiling
panels have been fully painted in gloss white. This allowed the
re-fitment of the repaired/repainted lighting wiring conduit and
the light fittings themselves. With completion of the ceiling
the curved panels above the luggage rack were able to be fitted.
32RM activity of late has been the complete re-wire of the
drivers No.2 end control console and re-wiring and repair of the
No 2 end marker lights. Some of the missing throttle control
components have also been made.
63RM: This car is running well. Apart from suffering from broken
windows the only problem to surface was some slight coolant
leaks on the RC engines.
DRC40: Running on its monthly Silver Streak commitments
with no real issues. The car has re-developed its occasional
transmission "slipping" problem.
2HH: All of the 4 doors have now been rebuilt by our Green Reserve
volunteers. The final re-built door waits re-fitment.
74RM: Work is going on with the major car body
rebuild. This has mainly involved completing the large amount of
straightening/filling work around the rear body section.
The railway has their own web site now and this can be
found from the ATR website. Go to the Adelaide River page
and click on the links.
The precinct at Adelaide River had a good
number of visitors for the picnic day this
year which is
held in August each year. Earlier in the month
150 visitors in the annual Rejex Rally visited and 150
people were fed by the railway.
The railway
has made a great effort to clear the right of way
of the former North Australian Railway. Set out below is a
report of work done.
"North
of the big bridge #139 good progress was being made with the
removal of trees that were either growing through our track or
very close to it. Peter Poole wielded his 1800 watt Makita
electric chainsaw in sensational fashion to down some very stout
trees (like African Mahogany). Jack Devlin hauled the logs to
the loading position using his 1800 cc Quad bike. From there we
used Jack’s trailer to take them to the dump. The NAR track is
now beautifully clear for more than 200m. Another Working Bee
will see it cleared back to the bridge. Its many thanks to
Peter and Adina Poole and Jack Devlin for this great effort.
Also thanks to Wayne Parsons for the loan of Wayne’s chainsaw."
Short Tom
progress.
"In
the last few days the protective shelter for the Short Toms has
been improved by completing the painting of the frame (with
“Machinery Grey”) and progressing the work on the side walls
which are open at the bottom for light and air. Some Alcinite
type clear sheeting would help if anyone has a spare sheet or
two.
Leo Izod did some good work in
straightening a set of end stairs that had been seriously bent
on Short Tom #86. And a renovated set of stairs was fitted to
Short Tom #450."
Altogether a huge project
to retain this part of Australia's rail
heritage.
Puffing Billy - Emerald Tourist Railway Board
The railway
has had a number of changes in the ETRB, the Statutory
Authority responsible for the operation of the railway.
For the first time the number of State Government
representatives equal the number of the representatives
nominated by
the PBPS. The PBPS has the right under the Emerald
Tourist Railway Act to submit to the
Government four persons as members of the Board. A
maximum of ten persons may be appointed to the
Board, the remainder being State Government representatives. Up
to now the number of Government Board members have
been restricted to three persons to allow the PBPS
have the majority on the Board should contentious
decisions arise.. The Board now has 8
members to allow additional skills to be
available to the Board.
The PBPS has introduced special badges to recognise 20,
30, 40, and 50 years of service to the Society.
A number of people very active in the railway have died in
2008 and the most recent passing was that of
Tom Kilner, who was the railway's Way and Works Manager.
Recently commemorated was the death of the railway's first
Enginemen's examiner, Reg Walton. The year 2008 has not
been kind to Puffing Billy
people.
The railway has purchased two DH diesels from McKay
Queensland. They have now arrived at Menzies
Creek on their way to Belgrave for
modification and for one engine to be re-gauged to 2'6".

DH at Menzies Creek
Photo J.
Frost
A special night time
run to Gembrook was held in June with some listening
stops on the way. A bus returned some passengers from Gembrook
to Belgrave.
Puffing Billy collects the postcodes of all
passengers as they enter the railway. As well as showing
where local people originate from, they also
show the success or otherwise of publicity in
overseas countries.
The railway has a number of Green Corp projects
going at the moment and works at Clematis and
the cosmetic restoration of a van at Menzies Creek is
progressing.
The restoration of the
Climax engine is going well with the chimney base casting
for the smoke box arriving and is now being worked on. The
chimney has been dismantled and repairs are under way. In
addition, many other works are also under way as part of the
restoration of this unique locomotive.
Locomotive 8A has achieved its century and this was
celebrated in the age old enginemen's way
by chalking the milestone on the smoke box
door.
Steamrail
Steamrail ran on the 14th June 2008 what was the
last steam powered trip from Melbourne to
Albury on the broad gauge tracks before they
are converted to standard gauge. The trip was plagued
by late running due to things beyond the control of
the organisers. In the end the trip was suspended early
the next day at Seymour at 2.09am instead of
it being back in Melbourne many hours earlier. At
that time of morning seven buses were obtained and ferried
the passengers back to the city. Part of the
delay was due to the train being forced to wait 2 1/2
hours in the night at Wangaratta on the way home, waiting to cross a
passenger train from Melbourne.
Electrail has been in discussions with
Connex to discern the requirements for Electrail to
operate once Steamrail gains its mainline accreditation. Electrail
has been unable to run any of its historic electric trains
for several years. In the meantime restoration of carriages has
continued with work being done on Swing door carriage 12BT
and Tait 341T. During the past open day at the depot
the electric stock was able to move under power to be
placed at the platform for display. Six Hitachi electric
cars were re-sold to the Government and have been
placed in suburban revenue service.
A series of steam hauled shuttles ran on the
Glen Waverly line in June and were enjoyed by the
public.
Work on A2 986 continues and
cracks to the cylinders revealed in boring have
been stitch welded. Diesel engine T364 is under
repair at Steamrail Newport and T395 at the EDI
workshops at Newport. Carriages 46BE has been
repainted and Goulburn sleeping car is having major
electrical modifications and plumbing alterations. 25BE
has had a general roof water proofing done and 500AK has had its
battery replaced. 1BCE has received a repaint and looks very
smart. 17BE also had roof repairs.
BZ269, which was purchased from West Coast
Railway, is being converted into a dance carriage. It will
have a retention toilet and the car will be fully refurbished.
it will run with Moorabool and will provide a great travel
experience for passengers to party in.
Standard gauge R766 engine is in NSW and is
moving towards completion of its conversion. The spare
boilers which were stored near the Tarp shop have
been moved over to West Block.
The Victorian Goldfields Railway
The railway has completed major repairs to
the Muckleford Creek Bridge and replaced three piles in the
structure. The stations platform at Castlemaine which is
an island platform serving both the Mainline trains and the Heritage
Railway has been resurfaced. Before the works were
done, a number of conduits for future signalling cabling were
installed. It was determined that
the best way to get the machines to do
the job and lay the hot mix was to load all the
material at Muckleford and run a goods train to the
heritage platform. This saved major problems for the contractor as
the rail service between Melbourne and Bendigo is now
intensive.
The level crossing at
Bendigo Road has received attention under the State Government's
ALCAM Programme and rumble strips have been installed on
the road surface.
The railway ran a
successful Friends of Thomas weekend in April but was forced to
abandon the proposed event in July. The owners of
the franchise, who are overseas, have placed such
heavy restrictions on the use of their intellectual
property that it is very difficult to run
Thomas Events. As they could not receive agreement
to run any Thomas events, they ran a successful
replacement children's day. Many Heritage railways in the
United Kingdom have also dropped running Thomas Events
because of this problem.
J515 over its life has a reputation for
starting fires and additional work has been done by
installing some new grids adjacent to the left hand side
ash pan dampers. The grids on the right hand side
are to be replaced in the future. In addition other mechanical
work has been done.
J541 has had a C exam carried out and
some minor work carried out. Some window glazing has been
done to 30 BCPL and restoration work done to 41 BU. 29 BCPL is
being readied to return to service with a final fit
out of seating.
On Saturday 26 July a gala day of double
headed J class engines was held.

Double J's arriving at Maldon
Photo Bob Wilson
Tramway Museum Society
The line near One Tree Hill has had an
upgrade with 16 new sleepers laid and the track lifted and
packed. More work is required on this section and additional
sleepers have been sourced.
Some site clearing has also been
done and an area near the house has been
leveled. Other spoil from works have been leveled and
the material removed to a fill on the low
lying ground between the depot fan and the main line
adjacent to the toilet block. Other material
will be used to re-surface the main entrance
and caretaker's roadways.
The kiosk has seen some carpentry
done to seal the back and sides of the new cupboard
to allow it to be installed.
Restoration of Q 199 and X2 680 continues.
199 has refurbished seats and panelling in
place and these came from car No 200. The colourfleck
paint on the ceiling, which the MMTB introduced as a
cost saving measure, has been removed to
reveal the varnished ceiling.
X2 680 now looks the best it has looked since
it ran at Footscray. New replacement builders plates have
been installed in Adelaide H 368. They were copied
by the Bendigo Tramway from an original plate in their tram No H
369.
Walhalla Goldfields Railway
Work has steadily proceeded on the new
accreditation procedures. The railway has recognised
the need to train new young people to
take over from the existing generation as they
retire, often for the second time. To do this teams have
been formed to allow the transfer of skills and
information.
The cost of running the railway was catching
up and it has been necessary for the first time for
many years to increase the fares. The Fowler
locomotive has started an overhaul and the Kasey engine
will take up the load as the railways
operating engine. The Class 10 diesel failed on its test run
and work has been suspended on this machine until a full
assessment is carried out. So far the engine
has cost the railway in excess of $139,000 and ten
years work.
As part of the usual work
required to keep all railways operational a
considerable amount of ballast has been
obtained and spread between Thomson and Walhalla.
The railway ran a successful
"Murder on the Walhalla Express" in May and 55 guests
enjoyed a three course meal and an "Agatha Christie"
evening.
Updated August 2008